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Daily Field Report
Observations/Finding
As requested, the site was visited by the AS Engerineering and Consulting (ASEC) representative noted above, for the purpose of providing quality control inspection and testing services, visual observation techniques were employed to assure compliance with project drawing/specifications, applicable codes, and materials submittals. the following observations were observed on site this day.
Contractor continued work on the dam keyway and the south side and north side of the keyway. Fill was placed and spread using a dozer and ground crew collecting and removing oversized materials. Compunction was performed using a D51pxi., sheeps-feet roller and dump truck.
Density testing was performed using a Troxler nuclear gauge (#3430, serial #29588).
Density testing result:
P-2 Moisture-Density Relationship (proctor) = 99.5 @ 22.1%
T1-elevation -9′ from top of keyway P-2, Yd 102.4, M%25.4, Compaction: 102.9%
T2-elevation -9′ from top of keyway P-2, Yd 104, M%23.1, Compaction: 104.5%
T3-elevation -9′ from top of keyway P-2, Yd 102.5, M%24.4, Compaction: 103%
T4-elevation -8.5′ from top of keyway P-2, Yd 102.1, M%25, Compaction: 102.6%