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Density Test Report

Date :12/16/2024
Project No :2024C202
Client Company :CCG
Arrival Time :12/16/2024 07:30
Onsite Hours :
Name of the Project :Old Griffin Rd - Hawthorne Reserve
Project Location :Dallas
Weather :Partly cloudy
Departure Time :12/16/2024
ASEC Technician Name :Solomon Cherie

Observations/Finding

Test Date Test Number Moisture Content (%) Dry Density (pcf) Proctor Number Max. Dry Density (pcf) Optimum Moisture (%) Compaction (%) Specified Compaction (%) ASTM Test Method Pass/Fail
12/16/2024 1 28.6 88.4 S-02 97.2 24.9 90.9 95 D6938 Fail
Location : Lot #115, Elv/Depth :4 feet below finished grade
Comment : It was determined the underlying soils were still moist/loose therefore, this layer needs to be removed and the underlying lift scarified and aerated. Gauge Serial No. :30942
12/16/2024 2 25.5 91.9 S-02 97.2 24.9 94.5 95 D6938 Fail
Location : Lot #115, Elv/Depth :4 feet below finished grade
Comment : Recompaction required prior to next lift placement. Gauge Serial No. :30942
12/16/2024 3 26.2 92.1 S-02 97.2 24.9 94.8 95 D6938 Fail
Location : Lot #114, Elv/Depth :3 feet below finished grade
Comment : Recompaction required prior to next lift placement. Gauge Serial No. :30942
12/16/2024 4 27 94.3 S-02 97.2 24.9 97.0 95 D6938 Pass
Location : Lot #115, Elv/Depth :4 feet below finished grade
Comment : Gauge Serial No. :30942
12/16/2024 5 23.9 92.7 S-02 97.2 24.9 95.4 95 D6938 Pass
Location : Lot #115, Elv/Depth :3 feet below finished grade
Comment : Gauge Serial No. :30942
Technician Signature / DateSolomon Cherie, December 16, 2024
Reviewer Name / DateKenneth Mosman, January 10, 2025