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Daily Field Report
Observations/Finding
As requested, a representative from AS Engineering and Consulting (ASEC) visited the site to perform quality control inspection and testing services. Visual observation techniques were employed to verify compliance with project drawings/specifications, applicable codes, and approved material submittals. The following observations were made during the site visit:
1. Earthwork Activities
Placement and compaction of backfill materials continued in the following areas:
- Sewer trench between MH4.1 and MH4.2.
At the time of arrival, our representative observed active work in progress. Fill material was being placed in 1-foot lifts and compacted using a 9-ton sheepsfoot roller and trench compactors.
2. Compaction Testing
Compaction testing was performed using a Troxler nuclear density gauge in accordance with ASTM D2937. Additionally, general probing was conducted using a 3/8-inch diameter probe rod.
Density test results indicated that many of the compacted materials did not meet the project specification of 95% of the maximum dry density, as determined by Standard Proctor ASTM D698.
Note: Moisture content exceeded the specified range limit and materials required scarification and aeration prior to replacement. The contractor was informed of this issue but did not take corrective action.
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